Final Report B733 (PK-YGW) Singapore Changi, 28 November 2020
Final Report B733 (PK-YGW) Singapore Changi, 28 November 2020
On 28 November 2020, a Boeing 737-300F taxiing for an early morning departure at Singapore Changi crossed an illuminated red stop bar in daylight and entered the active runway triggering an alert which enabled the controller to instruct the aircraft to immediately exit the runway and allow another aircraft already on approach to land. The Investigation found that the flight was the final one of a sequence of six carried out largely overnight as an extended duty predicated on an augmented crew. The context for the crew error was identified as a poorly managed operator subject to insufficient regulatory oversight.






