On 31 May 2014, a Gulfstream IV attempted to take off with the flight control gust locks engaged and, when unable to rotate, delayed initiating the inevitable rejected take off to a point where an overrun at high speed was inevitable. The aircraft was destroyed by a combination of impact forces and fire and all seven occupants died. The Investigation attributed the accident to the way the crew were found to have habitually operated but noted that type certification had been granted despite the aircraft not having met requirements which would have generated an earlier gust lock status warning.
Description
On 31 May 2014, a Gulfstream IV (N121JM) registered to SK Travel and being operated under lease by Arizin Ventures on a private business flight from Bedford MA to Atlantic City NJ initiated a high speed rejected take off in normal ground visibility at night and subsequently overran the end of the 2140 metre-long runway 11 by approximately 570 metres. During the overrun, the aircraft collided with ground obstructions before ending up in a gulley where a post crash fire consumed most of the aircraft wreckage. The three crew and four passengers died and the aircraft was destroyed.
The main aircraft wreckage (reproduced from the Official Report as credited to Massachusetts State Police)
Investigation
An Investigation was carried out by the NTSB. The FDR, CVR and QAR were recovered from the wreckage and data from all three was successfully downloaded. The QAR data covered 303 hours of data on 176 flights. A Preliminary Report on the initial progress of the Investigation was published on 13 June 2014.
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