On 10 April 2017, a Boeing 757-200 landing at Alicante in benign weather conditions was mishandled by an inexperienced First Officer on his third and final Line Check attempt and significant damage resulted from rear fuselage runway contact. The Investigation found that after an uneventful flight thus far, the Check Captain intervened to tell the First Officer to lower the nose after touchdown but on receiving a response indicating that he believed a go around was required, the Captain took control to complete the landing. The Investigation considered that the supervising Captain could have prevented the accident by intervening earlier.
Description
On 10 April 2017, a Boeing 757-200 (G-LSAI) being operated by Jet2.com on an international passenger flight from Leeds-Bradford to Alicante, during which the First Officer was undergoing a Final Line Check conducted by a Training Captain occupying the left seat observed by another Training Captain occupying the supernumerary crew seat, was mishandled during a day VMC landing and was subsequently found to have sustained significant damage after the rear fuselage struck the runway. None of the 238 occupants were injured but the runway surface was also marked.
Investigation
An Investigation into the Accident was carried out by the Spanish Commission for the Investigation of Accidents and Incidents (CIAIAC). Both the CVR and FDR were removed from the aircraft and downloaded but it was found that the 30 minutes of high quality CVR data had been overwritten because of a post flight delay in isolating the recorder, which was contrary to clear instructions in the Operations Manual (OM).
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