On 25 January 2016, an ATR 72-200 crew departing from and very familiar with Karup aligned their aircraft with the runway edge lights instead of the lit runway centreline and began take-off, only realising their error when they collided with part of the arrester wire installation at the side of the runway after which the take-off was rejected. The Investigation attributed the error primarily to the failure of the pilots to give sufficient priority to ensuring adequate positional awareness and given the familiarity of both pilots with the aerodrome noted that complacency had probably been a contributor factor.
Description
On 25 January 2016, an ATR 72-200 (OY-LHA) being operated by an unidentified airline on a scheduled domestic passenger flight from Karup to Copenhagen rejected its night take off in fog from the 2,929 metre-long runway 27L when the crew realised that they had aligned the aircraft with the right hand runway edge lights instead of the runway centreline lights. There were no injuries to the 69 occupants but minor damage was caused to the aircraft and six runway edge lights and two obstacle lights on a military arrestor cable mechanism at the side of the runway were destroyed.
Investigation
An Investigation was carried out by the Aviation Unit of the Danish Accident Investigation Board. The SSFDR and SSCVR were removed and their data were successfully downloaded and a recording of Karup TWR voice communications was also available.
It was found that the 38 year-old Captain, who had been PF for the take-off had accumulated 3,514 total flying hours including 1,134 hours on type and that the 35 year-old First Officer had accumulated 1,530 total flying hours including 390 hours on type. Both pilots were “very familiar” with the joint military/civil use aerodrome at Karup and were “often scheduled to fly the domestic route from Karup to Copenhagen”.
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